
Investigators have uncovered a chilling discovery within the preliminary investigation into the Air India Flight 171 crash which killed 260 individuals in June.
Simply seconds after takeoff, each the 12-year-old Boeing 787 Dreamliner’s fuel-control switches abruptly moved to the “cut-off” place, ravenous the engines of gas and triggering whole energy loss. Switching to “cut-off” is a transfer usually performed solely after touchdown.
The cockpit voice recording captures one pilot asking the opposite why he “did the cut-off”, to which the individual replies that he did not. The recording does not make clear who stated what. On the time of takeoff, the co-pilot was flying the plane whereas the captain was monitoring.
The switches have been returned to their regular inflight place, triggering automated engine relight. On the time of the crash, one engine was regaining thrust whereas the opposite had relit however had not but recovered energy.
Air India Flight 171 was airborne for lower than 40 seconds before crashing into a crowded neighbourhood within the western Indian metropolis of Ahmedabad, marking one in all India’s most baffling aviation disasters.
Investigators are probing the wreckage and cockpit recorders to know what went unsuitable simply after takeoff. The Air India flight climbed to 625 ft in clear climate earlier than shedding location knowledge 50 seconds in, per Flightradar24. Saturday’s 15-page report gives early insights.
The investigation – led by Indian authorities, with consultants from Boeing, GE, Air India and Indian regulators, alongside members from the US Nationwide Transportation Security Board and the UK – additionally raises various questions.
Investigators say the lever-lock gas switches are designed to stop unintentional activation – they have to be pulled as much as unlock earlier than flipping, a security characteristic courting again to the Fifties. Constructed to exacting requirements, they’re extremely dependable. Protecting guard brackets additional protect them from unintentional bumps.
“It could be virtually not possible to tug each switches with a single motion of 1 hand, and this makes unintentional deployment unlikely,” a Canada-based air accidents investigator, who wished to stay unnamed, advised the BBC.
That is what makes the Air India case stand out.
“It does beg the query: why did the pilot, any pilot, truly push the switches to the off place,” Shawn Pruchnicki, a former airline accident investigator and aviation professional at Ohio State College, stated.
“Was it intentional, or the results of confusion? That appears unlikely, because the pilots reported nothing uncommon. In lots of cockpit emergencies, pilots might press the unsuitable buttons or make incorrect picks – however there was no indication of such a state of affairs right here, nor any dialogue suggesting that the gas switches have been chosen by mistake. This type of error does not usually occur with out some evident problem,” he advised the BBC.

Peter Goelz, a former managing director of the US’s NTSB, echoed an analogous sentiment: “The discovering could be very disturbing – {that a} pilot has shut off the gas change inside seconds of flying.”
“There’s possible rather more on the cockpit voice recorder than what’s been shared. A lone comment like ‘why did you narrow off the switches’ is not sufficient,” he stated.
“The brand new particulars counsel somebody within the cockpit shut these valves. The query is, who, and why? Each switches have been turned off after which restarted inside seconds. The voice recorder will reveal extra: was the flying pilot making an attempt to restart the engines, or the monitoring one?”
Investigators imagine the cockpit voice recorder – with audio from pilot mics, radio calls and ambient cockpit sounds – holds the important thing to this puzzle.
“They have not recognized the voices but, which is essential. Sometimes, when the voice recorder is reviewed, individuals acquainted with the pilots are current to assist match voices. As of now, we nonetheless do not know which pilot turned the switches off and again on,” stated Mr Goelz.
Briefly, investigators say what’s wanted is obvious voice identification, a full cockpit transcript with labelled audio system, and an intensive evaluate of all communications from the second the airplane was pushed again from the gate to the time it crashed.
Additionally they say this underscores the necessity for cockpit video recorders, as beneficial by the NTSB. An over-the-shoulder view would present whose hand was on the cut-off change.
Earlier than boarding Flight 171, each pilots and crew handed breathalyser exams and have been cleared match to fly, the report says. The pilots, based mostly in Mumbai, had arrived in Ahmedabad the day earlier than the flight and had sufficient relaxation.
However investigators are additionally zeroing in on what they describe is an attention-grabbing level within the report.
It says in December 2018, the US Federal Aviation Administration issued a Particular Airworthiness Data Bulletin (SAIB) highlighting that some Boeing 737 gas management switches have been put in with the locking characteristic disengaged.
Whereas the problem was famous, it wasn’t deemed an unsafe situation requiring an Airworthiness Directive (AD) – a legally enforceable regulation to right unsafe circumstances in a product.
The identical change design is utilized in Boeing 787-8 plane, together with Air India’s VT-ANB which crashed. Because the SAIB was advisory, Air India didn’t carry out the beneficial inspections.

Mr Pruchnicki stated he is questioning whether or not there was an issue with the gas management switches.
“What does this [bit in the report] precisely imply? Does it imply that with a single flip, that change may shut the engine off and lower the gas provide? When the locking characteristic is disengaged, what precisely occurs? Might the change simply flip itself to off and shut down the engine? If that is the case, it is a actually severe problem. If not, that additionally must be defined,” he stated.
Others, nevertheless, aren’t satisfied it is a key problem.
“I have not heard of this which seems to be a low-profile FAA issuance. Nor have I heard any complaints [about the fuel switches] from pilots – who’re often fast to talk up. It is price analyzing because it’s talked about, however it might simply be a distraction,” stated Mr Goelz.
Capt Kishore Chinta, a former investigator with India’s Plane Accident Investigation Bureau (AAIB), wonders whether or not the switches tripped due to an issue with the airplane’s digital management unit.
“Can the gas cut-off switches be triggered electronically by the airplane’s digital management unit with out motion by the pilot? If the gas cut-off switches tripped electronically, then it is a trigger for concern,” he advised the BBC.
The report says gas samples from the refuelling tanks have been “passable”. Specialists had earlier steered gas contamination as a potential explanation for the twin engine failure. Notably, no advisory has been issued for the Boeing 787 or its GE GEnx-1B engines, with mechanical failure dominated out for now pending additional investigation.
It additionally stated that the plane’s Ram Air Turbine (RAT) had deployed – a transparent signal of a significant techniques failure – and the touchdown gear was present in “down place” or not retracted.
The RAT, a small propeller that extends from the underside of the Boeing 787 Dreamliner, acts as an emergency backup generator. It robotically deploys in flight when each engines lose energy or if all three hydraulic techniques register critically low stress, supplying restricted energy to maintain important flight techniques operational.
“The deployment of the Ram Air Turbine (RAT) strongly helps the conclusion that each engines had failed,” Mr Pruchnicki stated.
A Boeing 787 pilot defined why he thought the touchdown gear was not retracted.
“Today, each time I take off in a 787, I discover the touchdown gear retraction course of carefully. By the point the gear deal with is pulled, we’re already at about 200ft (60.9m), and your complete gear retraction course of completes by round 400ft – roughly eight seconds in whole, because of the plane’s high-pressure hydraulic system.”
The pilot believes the one flying had no time to assume.
“When each engines fail and the plane begins taking place, the response goes past simply being startled – you go numb. In that second, touchdown gear is not your focus. Your thoughts is on one factor: the flight path. The place can I put this plane down safely? And on this case, there merely wasn’t sufficient altitude to work with.”
Investigators say the crew tried to get well, but it surely occurred too quick.
“The engines have been switched off after which again on. The pilots realised the engines have been shedding thrust – possible restarting the left one first, adopted by the proper,” stated Mr Pruchnicki.
“However the proper engine did not have sufficient time to spool again up, and the thrust was inadequate. Each have been finally set to “run”, however with the left shut down first and the proper too late to get well, it was just too little, too late.”